I don't know if this will help or not, but the following is a chronological listing of what Lane has already done with related results, from Lane's posts (his quotes). Maybe it might jog people's memories or highlight something we've all missed:
9-27
I had noticed a increasing roughness over the last couple of months. Since then the car seems to run on about 3 1/2 cylinders - 3 good and one not completely out of it but not healthy. My first thought or course is clogged idle jet, but after a couple of removals and thorough cleanings I am not so sure, nor do I really want to remove them again. Could it be that the old adage or "Most carburetor problems are ignition problems" be true…… it is definitely cylinder #1, and it seems to be getting a weak or intermittent spark. It happens at all RPMs so it is unlikely that it's an idle jet.
Wires (8mm) and rotor ordered from PerTronix.
The Disti cap corrosion was only on #1 terminal and it was around the terminal, but not on the contact surface (cleaned and replaced)
10/3
When I got home from work some of the parts had arrived so I installed them. I now know somethings that the problem ISN'T. It's not:
- A bad spark plug on #1. I pulled #1 and #2 and they looked the same, so I swapped them.
- Carb base gaskets. Replaced 'em.
- Idle jets. Got four nice shiny new ones in there.
- Distributor cap. Pretty new one didn't help.
Rotor. Nope, that didn't help either.
To recap, the car seems to be running on 3 1/2 cylinders. Pulling the #1 plug wire has only a minimal effect on idle while pulling any other one damn near kills it. The car starts well enough and the misfire seems to be very consistent.
Carbs were synched and in tune before I felt the need to clean them due to running slightly rougher than they had been. I had them off to clean and I also pulled them so that I could remove the shroud and correct a rattle. Somewhere in there I changed the situation, but I am not sure where. At one point I removed the #1 plug wire to move it out of the way, and that makes me suspicious. I could have messed it up somehow.
I removed, disassembled, and cleaned out the carb for #1 and #2, and there was no change.
10/7
(After installing new plug wires)
It started up and sounded like all 4 cylinders were firing, but the deteriorated quickly. The symptoms are different, however. There were times when all four were firing, but it was intermittent, and seemingly only at higher RPMs. That sounds a bit like idle jets, but it isn't consistent. I have gotten the carbs as clean internally as I know how to do and really don't want to screw with them again.
Danny P. asked “what is your battery voltage at idle? Fuel pump pressure?”
10/8
To recap, I have replaced the following:
- Carb base gaskets
- Idle jets
- Distributor cap
- Rotor
- Plug wires
I have swapped the plugs from #1 and #2 and the problem appeared to stay at #1. I have also cleaned the air filters (they needed it).
After replacing the plug wires the problem appeared to go away for the first few seconds after I started the car. When it returned, it was less consistent, going away occasionally, usually when at higher RPM. I am becoming suspicious of the distributor itself. The coil is the Pertronix doohickey that matches the distributor.
10/9
Installed a new set of plugs, gapped at .028”
“Why does it start fine and sound good at first, deteriorating quickly over time?”
I have no way to check fuel pressure. I don't suspect this as the issue as the car will rev, but won't idle. The filters date from April.
10/10
There no longer appears to be a single offending cylinder, which is confusing. The problem now seems to happen after a few seconds of clean running.
I am still leaning toward ignition, but a collapsed line or filter (internally as both are relatively new metal ones) sounds plausible.
10/11
Installed a new coil – “Well the new coil didn't improve anything.”
I decided to check the carbs again and listened to the driver side one. There is a distinct "chuffing" sound from one cylinder so I removed, disassembled, and cleaned it again, with no effect.
(The fault) was specific to one cylinder (#1) for a while, but that has now changed. I am probably chasing at least two problems, at least one of which I probably caused when I removed some stuff to fix a rattle in the shroud.
The chuffing is on the #3-4 side. New base gasket. I suppose the manifold itself could be a little loose.
New carb base gaskets as of Wednesday. However, the manifold base gaskets are a whopping one year old and much harder to get to, so that's probably it.
10/12
As expected the valves are fine (and he replaced both head-to-manifold gaskets).
I believe what happened is that this was building for a while but I probably did mess up the spark plug wire on #1 when I was fixing the rattle in the shroud.
10/20
Replaced head-to-manifold gaskets (from Stan).
It will now idle and you can drive it below about 50 MPH, but the chuffing is still there and it still runs like s**t most of the time. It is possible that I broke the gasket on the 3/4 side installing it, so I am going to order some more and try again...
10/21
Valve clearance is perfect. I felt the gasket on the bad side give as I was putting it on, hence my concern about breaking it. If it's broken in the middle (my suspicion), the spray test won't show anything.
I whipped them off (carbs and manifolds) (I'm getting pretty good at it) only to discover that the existing gasket, although broken outside of one of the studs, was otherwise ok. It's unlikely that is the problem.
10/26/14
Neither borrowed compression tester would work so I went and bought one. I have a nice even 110 all around.
I put everything back together including a new manifold-to-head gasket and now the chuffing is gone. It started quickly and idled well. I revved it to 2000 RPM for about 30 seconds and it seemed smooth.
Turned it off and let it sit for 5 minutes.
went to take a test drive. Immediately off idle under load I could tell the problem was still there. I drove a few blocks with it running roughly to warm it up and could see that there was little if any improvement although it seems to idle just fine.
10/27
To recap:
Firing order is correct. All electrical parts in the ignition have been replaced except the ignitor module itself. Plugs gapped and all are firing. I have a simple T connection to the fuel line, after which it travels to each carb separately. Both carbs have been apart multiple times and all accessible passages blown out with compressed air. Fuel screens in carbs cleaned. New idle jets installed. Both fuel filters (metal type) replaced prior to Carlisle. New gas in the tank.
Anybody see anything significant in the fact that everything appears ok until I first apply a load to the engine as in backing out of the garage? May just be a coincidence.
10/8
I removed the module inside the distributor and found no corrosion, cleaned and replaced.
I started the car after buttoning it back up and it ran the same as it did when I turned it off on Sunday - poorly.
10/28
Danny P. is sending a Bosch 009 with installed Pertronics module to Lane to install and test. Lane will need to figure out how to get a coil to work with this Disti – His existing coil is made for his Pertronics disti and plugs may be different.
10/29
Justin doubts the new disti will solve things, Danny P. suspects fuel pressure. Lane (as yet) has no way to measure fuel pressure.