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It pains me to admit I am stumped but I am , read through this twice as I believe I have covered all of it.  Then comment with your thoughts.

....I purchased Speedster project with a 1600cc stock engine w/ single Solex carb, stock fuel pump, electronic 009 distributor, after- market Monza exhaust. Timing confirmed at 32 full advance. Started, ran, and idled decent performance going around the block. 

Pulled engine to freshen seals and detail  : Long block detailed new 36HP shroud, tins, new fuel pump, 009  distributor with electronic ignition, new cap, rotor, wires, FP regulator, switched to alternator, new dual baby Weber carbs and reinstalled engine . 3/4 side would not respond to the carb mixture screw adjustment,  also if I pulled # 3 wire the engine rpms did not drop off and here's where it gets crazy pulling # 1 wire........... did nothing either.   Compression test found :  # 1 cylinder -95lb.  and 2, 3 & 4 cylinders read 120 lbs.  SO there are  different things going on : the 3-4 side no mixture adjustment and pulling # 3 wire makes no difference...AND pulling # 1 wire rpms do not drop off but yet that 1 - 2 side does respond to carb mixture screw adjustment. I even switched carbs left to right and that did not change anything.

With # 1 cylinder at just 95 lbs.  decided to pull the engine taking it to a well know builder here in WV. for a rebuild

John ran the engine on a stand to confirm my issues,  he did a 2nd compression and leak down test, found leak down issues and  rebuilt engine.  1st cut with virgin existing AH case , cam and lifers, rockers , push rods all good as well as oil pump good too. Reground crankshaft, new bearings , 1641cc piston /cylinder set, new stock heads.

Reassembled and the same thing issues !   Pulling # 1 ignition wire issue as well as pulling # 3 wire no response and no 3 & 4 side mixture screw adjustment...it's still there. 

Also switched out distributor, car, rotor, coil,  plugs wires too.

Pulled the new carbs disassembled and checked for debris or obstructions then reinstalled. Also re-measured cam op (exhaust valves open & closed with dial indicator all specs as new) Checked for manifold leaks, gaskets etc.  ..... Opinions ?

 

Last edited by Alan Merklin
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Real puzzler. I've seen brand new Kadrons with a split emulsion tube or missing air passage brass plug cause one side not to respond to mixture settings.  But, you've switched the carbs and didn't see any difference, that is not the problem.

Is it possible that both carbs are running really lean (jets?, filter? pump?)? Perhaps the front to back runner differences would cause 1 &  3 to be leaner than 2 & 4 under very lean conditions?  I keep coming back to carbs, but the 1 & 3 is puzzling.

You flipped sides with the carbs with no result, so it’s not them, but did you flip the intake manifolds with the carbs or leave the manifolds in place and just flip the carbs?  I could suspect the intake manifolds or gaskets.

Is compression # now the same on all four cyls?

Is the idle even at 800-ish or does it look ragged?

Is there an obstruction in the fuel line for #3 & 4?  (I’m reminded of a piece of laytex glove in mine)

When you remove a plug wire and nothing happens at idle, what happens if you rev it?  Does it spin up roughly?  Does it spin up better with all plugs/wires connected or act the same on acceleration with #1 & 3 disconnected?

I keep suspecting the intake manifolds or gaskets, but.....

What is the alternator voltage output when you rev it up?  When you went from generator to alternator did you wire the old regulator by-pass right?

That’s all I’ve got right now.

Yes checked spark it's good at all plugs

 

Compression same on all "new"  four cylinders

Idles fine and revs fine on test stand

It's not intake / gaskets these were carefully rechecked visibly with carb cleaner and even sanded the intake and carb bases with emery cloth across a piece of glass in a figure 8 pattern (old school method) 

.........Interesting re: alt volts I  will check

And BTW we pulled the used exhaust off to see if there was dead occupants or remains there of.

Last edited by Alan Merklin
Alan Merklin posted:

... re-measured cam op (exhaust valves open & closed with dial indicator all specs as new) 

The fact that 1 and 3 share symptoms tends to make me think this is a cam issue. As you know, it’s either spark, fuel, or mechanical. You’ve swapped carbs side to side, and the problem persisted. You’ve paid a lot of attention to the ignition, without success.

You seem to be saying that you checked the exhaust valve with a dial indicator. Did you by chance check the intake?

Stan.. I'll rule out mechanical as most components are new.  Yes cam checked all lobes intake - exhaust and at specs ..   Since the engine is on a run stand a 140 miles from me we are going back and forth checking the boxes. The builder is going to test swap the duals carbs for a used stock manifold and Solex and see what happens.   I've com across some really strange issues over the years but this one tops it all.

Last edited by Alan Merklin

You know, somewhere in the back of my mind I remember hearing about something like this happening to someone else - like the engine idles on 2 cylinders but acts normally when you rev it or under load.  Don’t know if they used baby Webers or Kadron single throats, though, and there was no clear solution, other than swapping out the carbs to something else, which is where you’re going.

The brand new Brocar carb I put in the 1600 last year would not run at idle. Almost any idle. I could rev it non-stop to keep it running. It turned out that the idle pilot, (not the idle bypass or adjustment) screw was bottomed out and not allowing idle fuel into the mixture. This is the tiny screw that is mostly hidden on the right side of the carb body.  I had to spin down a tiny washer to “space” that pointed screw out of the fully seated position. I read about the issue on The Samba site. Many hours were wasted trying to adjust a very simple carb! Yikes, the MADNESS was present! Let’s make all of our replacement parts in third world countries where quality control has no meaning! ;-0 

One of the two guys I know who had problems with those carbs said that the passage for the idle circuit was non existent. The other said that the transition ports were not drilled in one of his carbs.  I don't know which it was but he said that the threads for the fuel line connection were stripped or not threaded as well. That part was fixed but the other issues clinched the rejection of the use of the carb set.

On another note. One time I replaced a turn signal switch assy. because of some reason I don't recall but when I installed the new switch and wiring harness, I stripped and grounded out the same wire in the new harness. Of course you KNOW the NEW assembly IS GOOD ! After a couple days of struggling with this same problem, you start changing everything else to no avail.  The shotgun approach !  Even that didn't get results. SOoooo.......I handed the job off to another guy. He did the proper diagnosis and determined that there was a grounded wire. Replaced the Switch assembly, and everything was fine !  The new switch I installed had the same wire skinned as the original wire. I ate crap for a while from the other guys..........Bruce

It wasn't me....I just knew someone that had similar problems. They figured it out.  I just paid attention.  I'm just glad you found a definitive source of your symptoms. It can be very frustrating sometimes. A plastic sandwich bag floating around in your fuel tank will drive you nuts too !!  How bout diesel fuel in the "cold start" gasoline tank on a Propane fueled truck ?..........Bruce

A few responses were spot on ( Thanks! ) and helped to resolve this two fold problem.   It juts baffled me that one side would not respond to a mixture screw adjustment and at idle # 1 and # 3 would not drop off in rpm's when those plug wires were pulled....  Be as it may and with poor Chinese workmanship, the  idle circuit passage and the transition ports were not drilled in one of the dual EPC 34 carbs.  Also because of a poor design the 1 and 3 cylinders are getting a very lean fuel mixture at idle.  Confirming that was easy, we bolted up a VW stock manifold single stock carb and it hummed along . I'm getting the one bad carb replaced under warranty. In many past applications I have had good luck with these EMPI  EPC single throat dual carbs, but I am so done with them.  BTW the Weber ICT 34 is the same thing...I would not suggest using these carbs . After doing a lot of research I would suggest two stock VW carbs on shorty manifolds with the twist linkage.

Last edited by Alan Merklin

Are they Weber 34 ICT's?  IF so there are quite a few of those and the Empi EPC 34's that have internal casting issues,..... idle circuit passage and the transition ports not drilled properly.  Also, the bottom of carbs and manifolds the surfaces are no exactly flat and have to be sanded by using a emery paper on a piece of glass in a figure 8 movements to get and exact flat surface. The throat on the carb where the cone air filter is clamped is tapered after the engine gets hot a few tomes the air filters slip off. Also there is no room the bottom manifold too head studs to get a wench on a 11mm nut so that area needs a light grinding to make room for a wrench or socket.

 

Last edited by Alan Merklin
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